I only had a few hours on Saturday, so the plan was to drill the holes for the power steering reservoir and test it with the engine running, then hopefully get some more time a bit later in the night to do some more. With the reservoir mounted, I filled it right to the brim ready to fill the empty pipes, then got the engine ready to fire again as I have now fitted the new street and performance headers. I’d welded, painted and fitted the steering linkage one night in the week, so it was all going in hopefully to stay. I pulled all the plugs and re-gapped them for the blower and the MSD, and tightened up the headers and moved a few cables that were now in the way with the new run. A quick double check, then check again, and it was ready to fire. It started easily as it always does, and sounded superb. Power steering works as expected, and no leaks that I can see which is good. A quick top up of the fluid and thats another one off the list.

The next thing I wanted to do was the horn button. Easy eh?. I put the assembly back together and tested it, and there was no way to get the signal from the Flaming River rack to the button. I left it and went and had my tea, then went back out to have another quick look at it. I ended up drilling two small holes and soldering a wire between the two so that the button on the wheel would work. A quick test fit, and it didnt work, which I convinced myself was a bad earth, so tightened the centre bolt. It was then I realised I’d put the spring on the wrong side of the contact plate and it was pushing it away from the contact. The wheel was on solid, and I had no puller. I yanked it, tapped it gently, and tried to use the screw holes in the wheel to get it off with no luck for 4 hours. I was desperately trying not to chip the paint, but it wasnt budging. After bending 3 or 4 bolts trying to shift it, I cut down a bracket by hand and filed it to make a puller and off it popped. I re-made the wire just in case I’d broken it, and fitted it this time making sure it worked properly before tightening it down. It was now 2am and I was knackered. Sunday I wired up the horns themselves, which sound great and had a massive tidy up before working on the F100 which is off to be blasted tomorrow. Funny how the easy jobs can take so much time!
